Process improvement using six sigma methodology

The purpose of this thesis is to solve the screw stuck issue of Sensor Module in Agilent Technologies, using Six Sigma methodology D-M-A-I-C. The current yield loss due to this defect had contributed to the increased production cost due to higher material scrap and rework time. Project objectives we...

詳細記述

保存先:
書誌詳細
第一著者: Chew, Li Ling
フォーマット: 学位論文
言語:English
出版事項: 2009
主題:
オンライン・アクセス:http://eprints.utm.my/id/eprint/123/1/ChewLiLingMFKM2009.pdf
http://eprints.utm.my/id/eprint/123/
タグ: タグ追加
タグなし, このレコードへの初めてのタグを付けませんか!
id my.utm.123
record_format eprints
spelling my.utm.1232018-01-29T06:54:42Z http://eprints.utm.my/id/eprint/123/ Process improvement using six sigma methodology Chew, Li Ling TJ Mechanical engineering and machinery The purpose of this thesis is to solve the screw stuck issue of Sensor Module in Agilent Technologies, using Six Sigma methodology D-M-A-I-C. The current yield loss due to this defect had contributed to the increased production cost due to higher material scrap and rework time. Project objectives were set in Define phase to increase the yield of both functionality and reworkability of Sensor Module from current baseline yield to 99.4% (targeted four sigma). The baseline data was collected in the Measure phase and shows that baseline yield for functionality and reworkability was 74% and 62% respectively. Analyze phase results revealed the relationship of vital few causes to the screw stuck issue, which led to the defect s root cause as thread galling. Thread galling phenomena was associated with the fasteners material and torque speed (rpm), therefore the relationship between these factors and the functionality and reworkability yield was developed. In Improve phase, the solution was chosen to replace the fastener s material and reduce the torque speed considering factors such as effectiveness, cost and lead time. Optimization test or DOE was carried out to determine the best options on the fastener s material selection and the torque speed. Experiment reveals improved yield with SP series nut new type, wax coated stainless steel screw, and manual torque driver. Pilot run was conducted successfully with 100% yield on functionality. In final Control phase, all the changes and implementation were institutionalized with proper training, documentation, process monitoring, response plan and sustainability plan. The result from the project has provided an insight on actual successful deployment of Six Sigma methodology DMAIC with application of its various statistical tools and techniques, and as the systematic problem solving framework on solving actual industrial issues. 2009-05 Thesis NonPeerReviewed application/pdf en http://eprints.utm.my/id/eprint/123/1/ChewLiLingMFKM2009.pdf Chew, Li Ling (2009) Process improvement using six sigma methodology. Masters thesis, Universiti Teknologi Malaysia, Faculty of Mechanical Engineering.
institution Universiti Teknologi Malaysia
building UTM Library
collection Institutional Repository
continent Asia
country Malaysia
content_provider Universiti Teknologi Malaysia
content_source UTM Institutional Repository
url_provider http://eprints.utm.my/
language English
topic TJ Mechanical engineering and machinery
spellingShingle TJ Mechanical engineering and machinery
Chew, Li Ling
Process improvement using six sigma methodology
description The purpose of this thesis is to solve the screw stuck issue of Sensor Module in Agilent Technologies, using Six Sigma methodology D-M-A-I-C. The current yield loss due to this defect had contributed to the increased production cost due to higher material scrap and rework time. Project objectives were set in Define phase to increase the yield of both functionality and reworkability of Sensor Module from current baseline yield to 99.4% (targeted four sigma). The baseline data was collected in the Measure phase and shows that baseline yield for functionality and reworkability was 74% and 62% respectively. Analyze phase results revealed the relationship of vital few causes to the screw stuck issue, which led to the defect s root cause as thread galling. Thread galling phenomena was associated with the fasteners material and torque speed (rpm), therefore the relationship between these factors and the functionality and reworkability yield was developed. In Improve phase, the solution was chosen to replace the fastener s material and reduce the torque speed considering factors such as effectiveness, cost and lead time. Optimization test or DOE was carried out to determine the best options on the fastener s material selection and the torque speed. Experiment reveals improved yield with SP series nut new type, wax coated stainless steel screw, and manual torque driver. Pilot run was conducted successfully with 100% yield on functionality. In final Control phase, all the changes and implementation were institutionalized with proper training, documentation, process monitoring, response plan and sustainability plan. The result from the project has provided an insight on actual successful deployment of Six Sigma methodology DMAIC with application of its various statistical tools and techniques, and as the systematic problem solving framework on solving actual industrial issues.
format Thesis
author Chew, Li Ling
author_facet Chew, Li Ling
author_sort Chew, Li Ling
title Process improvement using six sigma methodology
title_short Process improvement using six sigma methodology
title_full Process improvement using six sigma methodology
title_fullStr Process improvement using six sigma methodology
title_full_unstemmed Process improvement using six sigma methodology
title_sort process improvement using six sigma methodology
publishDate 2009
url http://eprints.utm.my/id/eprint/123/1/ChewLiLingMFKM2009.pdf
http://eprints.utm.my/id/eprint/123/
_version_ 1643643005386620928
score 13.153044