To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis

This case study demonstrates lean-based alternatives to conventional problem solving:- a step-by-step procedure to implement root cause analysis in a garment manufacturing factory working on an overhead hanger-based unit production system in the sewing lines. The objective was to increase the first-...

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Main Author: Garg, Yuvraj
Format: Conference or Workshop Item
Language:English
Published: 2022
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Online Access:https://repo.uum.edu.my/id/eprint/30695/1/7th%20ICSC%202022%20283-308.pdf
https://repo.uum.edu.my/id/eprint/30695/
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spelling my.uum.repo.306952024-04-02T11:23:59Z https://repo.uum.edu.my/id/eprint/30695/ To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis Garg, Yuvraj HD28 Management. Industrial Management This case study demonstrates lean-based alternatives to conventional problem solving:- a step-by-step procedure to implement root cause analysis in a garment manufacturing factory working on an overhead hanger-based unit production system in the sewing lines. The objective was to increase the first-hour production efficiency and to decrease the “off-standard time” of the sewing production line for the fivepocket trousers manufacturing unit. The primary study involves a capacity study on the sewing operations, a root cause analysis; an optimization of the work-in-process leftover from the previous shift at the start; and an action plan to solve the major causes identified in the root cause analysis. The major factors from root cause analysis were: high “off standard time”, less/nonuniform low initial work-in-process leftover by the previous shift, operator idleness, start delay by operators, operator absenteeism, The implementation was done with the help of training, coordinating, optimizing the in-process inventory at the start of the shift, and implementing an action plan. The execution led to an increase in first-hour production efficiency of the sewing line to 74% from 43.7%; a decrease in the “off standard time” of the sewing line to 7.6% from 14.8%; an increase in the production efficiency of to 90.68% from 80.75%. 2022 Conference or Workshop Item PeerReviewed application/pdf en https://repo.uum.edu.my/id/eprint/30695/1/7th%20ICSC%202022%20283-308.pdf Garg, Yuvraj (2022) To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis. In: 7th International Case Study Conference, 13 - 15 September 2022, Raia Hotel & Convention Centre, Terengganu, Malaysia.
institution Universiti Utara Malaysia
building UUM Library
collection Institutional Repository
continent Asia
country Malaysia
content_provider Universiti Utara Malaysia
content_source UUM Institutional Repository
url_provider http://repo.uum.edu.my/
language English
topic HD28 Management. Industrial Management
spellingShingle HD28 Management. Industrial Management
Garg, Yuvraj
To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis
description This case study demonstrates lean-based alternatives to conventional problem solving:- a step-by-step procedure to implement root cause analysis in a garment manufacturing factory working on an overhead hanger-based unit production system in the sewing lines. The objective was to increase the first-hour production efficiency and to decrease the “off-standard time” of the sewing production line for the fivepocket trousers manufacturing unit. The primary study involves a capacity study on the sewing operations, a root cause analysis; an optimization of the work-in-process leftover from the previous shift at the start; and an action plan to solve the major causes identified in the root cause analysis. The major factors from root cause analysis were: high “off standard time”, less/nonuniform low initial work-in-process leftover by the previous shift, operator idleness, start delay by operators, operator absenteeism, The implementation was done with the help of training, coordinating, optimizing the in-process inventory at the start of the shift, and implementing an action plan. The execution led to an increase in first-hour production efficiency of the sewing line to 74% from 43.7%; a decrease in the “off standard time” of the sewing line to 7.6% from 14.8%; an increase in the production efficiency of to 90.68% from 80.75%.
format Conference or Workshop Item
author Garg, Yuvraj
author_facet Garg, Yuvraj
author_sort Garg, Yuvraj
title To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis
title_short To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis
title_full To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis
title_fullStr To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis
title_full_unstemmed To Improve First-Hour Sewing Production Efficiency for a Garment Manufacturing Factory Using the Lean Problem-Solving Tool, Root Cause Analysis
title_sort to improve first-hour sewing production efficiency for a garment manufacturing factory using the lean problem-solving tool, root cause analysis
publishDate 2022
url https://repo.uum.edu.my/id/eprint/30695/1/7th%20ICSC%202022%20283-308.pdf
https://repo.uum.edu.my/id/eprint/30695/
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score 13.213126