Design And Development Of Gas Argon Purging System

Using a single pneumatic control valve with PI feedback controllers test, a method is proposed to design and develop to the current gas argon purging system while to identify that the present 6 different kinds of digital control valve may not give the actual flow rate to the liquid steel purgi...

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Main Author: Ooi, Seng Yeong
Format: Monograph
Language:English
Published: Universiti Sains Malaysia 2006
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Online Access:http://eprints.usm.my/58174/1/Design%20And%20Development%20Of%20Gas%20Argon%20Purging%20System_Ooi%20Seng%20Yeong.pdf
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spelling my.usm.eprints.58174 http://eprints.usm.my/58174/ Design And Development Of Gas Argon Purging System Ooi, Seng Yeong T Technology TJ Mechanical engineering and machinery Using a single pneumatic control valve with PI feedback controllers test, a method is proposed to design and develop to the current gas argon purging system while to identify that the present 6 different kinds of digital control valve may not give the actual flow rate to the liquid steel purging system. In the present work, a method is proposed, by incorporating the ABB PLC (Programmable Logic Controller) to explain how well the purging control system is being controlled. A method is proposed to estimate the accuracy of the system by implementing PI algorithm. Two MatLab simulation results are given on stable first second order and third order plus unity feedback transfer function models. The estimated PI models are compared with the real time implementation of PI controller in gas argon purging system. PI controllers are designed for the identified model and for the actual system. The proposed method gives performance close to that of the actual system. Using an appropriate pneumatic control valve is much concerned in this test by calculating out its coefficient of valve (Cv) by mean to identify higher flow rate may require higher value in Cv while lower flow rate requests for lower Cv. By the way, a test shows that by using wrongly control valve, the PI controller would produce intangible result. Using AMPL (ABB Master Program Language) with ABB PLC controller is much different from Siemens or Mitsubishi PLC programming which they intended to use ladder diagram as function for the control system. AMPL is used in two ways of connection of its programming, first is Data Base, and second is PC element. Data Base is held on intermediate between PC element and hardware’s(input card and output card of PLC) connection. Mircosoft Workgroup 3.11 operating system is used to transfer the AMPL programming to the PLC. 2 analogue signals and 4 digital signals are used in the program to manipulate the control system. The analogue signals will be connected to analogue input card and output card while digital signal will be placed at only digital input card, because there are 4 digital input signals can be used to generate 16 steps setting for the gas purging system. The PI controller designed on the system identified by the proposed method gives a performance better than the present working system. Universiti Sains Malaysia 2006-03-31 Monograph NonPeerReviewed application/pdf en http://eprints.usm.my/58174/1/Design%20And%20Development%20Of%20Gas%20Argon%20Purging%20System_Ooi%20Seng%20Yeong.pdf Ooi, Seng Yeong (2006) Design And Development Of Gas Argon Purging System. Project Report. Universiti Sains Malaysia, Pusat Pengajian Kejuruteraan Mekanikal. (Submitted)
institution Universiti Sains Malaysia
building Hamzah Sendut Library
collection Institutional Repository
continent Asia
country Malaysia
content_provider Universiti Sains Malaysia
content_source USM Institutional Repository
url_provider http://eprints.usm.my/
language English
topic T Technology
TJ Mechanical engineering and machinery
spellingShingle T Technology
TJ Mechanical engineering and machinery
Ooi, Seng Yeong
Design And Development Of Gas Argon Purging System
description Using a single pneumatic control valve with PI feedback controllers test, a method is proposed to design and develop to the current gas argon purging system while to identify that the present 6 different kinds of digital control valve may not give the actual flow rate to the liquid steel purging system. In the present work, a method is proposed, by incorporating the ABB PLC (Programmable Logic Controller) to explain how well the purging control system is being controlled. A method is proposed to estimate the accuracy of the system by implementing PI algorithm. Two MatLab simulation results are given on stable first second order and third order plus unity feedback transfer function models. The estimated PI models are compared with the real time implementation of PI controller in gas argon purging system. PI controllers are designed for the identified model and for the actual system. The proposed method gives performance close to that of the actual system. Using an appropriate pneumatic control valve is much concerned in this test by calculating out its coefficient of valve (Cv) by mean to identify higher flow rate may require higher value in Cv while lower flow rate requests for lower Cv. By the way, a test shows that by using wrongly control valve, the PI controller would produce intangible result. Using AMPL (ABB Master Program Language) with ABB PLC controller is much different from Siemens or Mitsubishi PLC programming which they intended to use ladder diagram as function for the control system. AMPL is used in two ways of connection of its programming, first is Data Base, and second is PC element. Data Base is held on intermediate between PC element and hardware’s(input card and output card of PLC) connection. Mircosoft Workgroup 3.11 operating system is used to transfer the AMPL programming to the PLC. 2 analogue signals and 4 digital signals are used in the program to manipulate the control system. The analogue signals will be connected to analogue input card and output card while digital signal will be placed at only digital input card, because there are 4 digital input signals can be used to generate 16 steps setting for the gas purging system. The PI controller designed on the system identified by the proposed method gives a performance better than the present working system.
format Monograph
author Ooi, Seng Yeong
author_facet Ooi, Seng Yeong
author_sort Ooi, Seng Yeong
title Design And Development Of Gas Argon Purging System
title_short Design And Development Of Gas Argon Purging System
title_full Design And Development Of Gas Argon Purging System
title_fullStr Design And Development Of Gas Argon Purging System
title_full_unstemmed Design And Development Of Gas Argon Purging System
title_sort design and development of gas argon purging system
publisher Universiti Sains Malaysia
publishDate 2006
url http://eprints.usm.my/58174/1/Design%20And%20Development%20Of%20Gas%20Argon%20Purging%20System_Ooi%20Seng%20Yeong.pdf
http://eprints.usm.my/58174/
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score 13.209306