Root cause failure analysis of final superheater tube from a coal fired power station

This paper presents the root cause failure investigation ot final superheater tube of unit 5 Stesen Janaelektrik Sultan Salahuddin Abdul Aziz (SJSSAA) Kapar or better known as Kapar Energy Venture (KEV). KEV is the largest power plant in Malaysia with a generation capacity of 2420 MW and the only po...

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Main Authors: Rahman M.M., Omar A.A., Ahmad J.
Other Authors: 55328831100
Format: Article
Published: Microscopy Society of Malaysia 2023
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spelling my.uniten.dspace-300782023-12-29T15:44:21Z Root cause failure analysis of final superheater tube from a coal fired power station Rahman M.M. Omar A.A. Ahmad J. 55328831100 57208577114 57210531371 Coal fired power plant Mechanical properties Microstructure Root cause failure investigation This paper presents the root cause failure investigation ot final superheater tube of unit 5 Stesen Janaelektrik Sultan Salahuddin Abdul Aziz (SJSSAA) Kapar or better known as Kapar Energy Venture (KEV). KEV is the largest power plant in Malaysia with a generation capacity of 2420 MW and the only power station in Malaysia with triple fuel filing capability, i.e.. gas. oil. and coal. Boiler unit 5 at KEV uses coal to operate in generating 500 MW of electricity. On 25 November 2011. final superheater tube failed at unit 5 plant (u5 FSH P2T5). A fish mouth fracture was visible at the failed surface of the tube. The material type of the tube is ASM213 T91. The failed tube was sent for identification of the root cause failure. The investigation was conducted through (i) visual inspection, (ii) non destructive testing, (iii) hardness measurement, (iv) bending strength measurement, (v) microstructure evaluation, and (vi) Larson Miller Analysis for oxide scale temperature calculation and life assessment of the tube. After the investigation was done, there was no evidence suggesting that this tube ruptured because of overheating. From the oxide scale temperature calculation, the metal temperature of the tube was about 534.32 �C which did not exceed the design temperature. After revisiting the power plant and conducting a thorough investigation, it was revealed that a malfunctioned soot blower was located near the failed tube. The steam from the malfunctioned soot blower was hitting the failed tube continuously causing the surface of the tube to loose its ductility and strength. The internal pressure forced the mbe to rupture and burst. Microstructures of the affected area help to identify one of the causes of the failure. � 2019, Microscopy Society of Malaysia. All rights reserved. Final 2023-12-29T07:44:21Z 2023-12-29T07:44:21Z 2013 Article 2-s2.0-85065178767 https://www.scopus.com/inward/record.uri?eid=2-s2.0-85065178767&partnerID=40&md5=3d472fcc71a33ea1b0f7cf0286db6073 https://irepository.uniten.edu.my/handle/123456789/30078 9 1 73 76 Microscopy Society of Malaysia Scopus
institution Universiti Tenaga Nasional
building UNITEN Library
collection Institutional Repository
continent Asia
country Malaysia
content_provider Universiti Tenaga Nasional
content_source UNITEN Institutional Repository
url_provider http://dspace.uniten.edu.my/
topic Coal fired power plant
Mechanical properties
Microstructure
Root cause failure investigation
spellingShingle Coal fired power plant
Mechanical properties
Microstructure
Root cause failure investigation
Rahman M.M.
Omar A.A.
Ahmad J.
Root cause failure analysis of final superheater tube from a coal fired power station
description This paper presents the root cause failure investigation ot final superheater tube of unit 5 Stesen Janaelektrik Sultan Salahuddin Abdul Aziz (SJSSAA) Kapar or better known as Kapar Energy Venture (KEV). KEV is the largest power plant in Malaysia with a generation capacity of 2420 MW and the only power station in Malaysia with triple fuel filing capability, i.e.. gas. oil. and coal. Boiler unit 5 at KEV uses coal to operate in generating 500 MW of electricity. On 25 November 2011. final superheater tube failed at unit 5 plant (u5 FSH P2T5). A fish mouth fracture was visible at the failed surface of the tube. The material type of the tube is ASM213 T91. The failed tube was sent for identification of the root cause failure. The investigation was conducted through (i) visual inspection, (ii) non destructive testing, (iii) hardness measurement, (iv) bending strength measurement, (v) microstructure evaluation, and (vi) Larson Miller Analysis for oxide scale temperature calculation and life assessment of the tube. After the investigation was done, there was no evidence suggesting that this tube ruptured because of overheating. From the oxide scale temperature calculation, the metal temperature of the tube was about 534.32 �C which did not exceed the design temperature. After revisiting the power plant and conducting a thorough investigation, it was revealed that a malfunctioned soot blower was located near the failed tube. The steam from the malfunctioned soot blower was hitting the failed tube continuously causing the surface of the tube to loose its ductility and strength. The internal pressure forced the mbe to rupture and burst. Microstructures of the affected area help to identify one of the causes of the failure. � 2019, Microscopy Society of Malaysia. All rights reserved.
author2 55328831100
author_facet 55328831100
Rahman M.M.
Omar A.A.
Ahmad J.
format Article
author Rahman M.M.
Omar A.A.
Ahmad J.
author_sort Rahman M.M.
title Root cause failure analysis of final superheater tube from a coal fired power station
title_short Root cause failure analysis of final superheater tube from a coal fired power station
title_full Root cause failure analysis of final superheater tube from a coal fired power station
title_fullStr Root cause failure analysis of final superheater tube from a coal fired power station
title_full_unstemmed Root cause failure analysis of final superheater tube from a coal fired power station
title_sort root cause failure analysis of final superheater tube from a coal fired power station
publisher Microscopy Society of Malaysia
publishDate 2023
_version_ 1806427549219160064
score 13.214268